Peter Leibert's Page
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The
Army
One of my
assignments at Northrop was to head a group called the Machinery Monitoring
Unit. Our charge was to pursue
contracts for test systems that would be capable of testing machinery using the
technology that had been developed for our navy programs, including the Polaris
missile testing work, and the commercial vehicle testing section of a subsidiary
of the Northrop Anaheim division. This was actually
a very interesting area. During the
late 1960s and early 1970s relatively little attention was being given to making
it easy to maintain machinery. We
did find some engine and vehicle manufacturers that were experimenting with
building-in some sensors, but very, very little of these approaches ever made it
into the designs for production units. The two companies
that seemed to be the leaders in having engineers give more priority to
maintainability were Volkswagen and Cummins.
Both had work going on in their laboratories targeted at improving access
to internal pressure and electrical information concerning the health of an
engine. The work of both companies
was focused on performance tests, how well the engine was working, and not
directly aimed at diagnosing what was the part that actually was causing a loss
in performance. Volkswagen also
was trying to develop a diagnostic tool to assist the mechanic to determine what
replaceable part was causing a lost in engine performance.
Cummins was trying to improve physical and electrical assess to
performance information for their future engines.
In other words, how could the production design of the physical engine be
altered to make it easier to obtain maintenance and performance data?
These companies
were very interested in working with us, as most of the engine manufacturer
engineers were mechanically oriented and our group of engineers were more
electrically oriented. We also had
a lot more experience in working with the sensors that could translate
mechanical information into meaningful electrical signals. It was not long
before three or four of us Northrop engineers were attending a Cummins technical
course about how their engines worked and how to maintain them.
I found it to be very interesting and I am sure that all of us learned a
lot. By the time their engine
course was completed, we had jointly developed a number of possible schemes for
conducting performance and diagnostic tests on a Cummins engine.
We had even identified existing sensors and mounts that might potentially
be used for obtaining the information about various pressure points, vibration,
rotation data and a number of additional parameters. In parallel, we
set up an engine lab in our Anaheim plant and were starting to conduct some
tests to learn more about the characteristics of various types of sensors when
used in that mechanical environment. During the
timeframe when we were performing these efforts to get ourselves smart about the
testing of various mechanical systems, corporate headquarters of Northrop
contacted the division General Manager with a request.
Some engineer had designed and built a new type of engine, which was
supposedly very simple, could be built for half the cost as equivalent current
engines, and had all kinds of other benefits.
Now he was approaching Northrop Corporate with a suggestion that they
invest. Corporate wanted our
“machinery experts” to test the engine and provide corporate with an
evaluation. The device was referred
to as a rotary engine. The next morning
in comes this guy with a big cardboard box and plops it on my desk.
He opens the box up to show us his engine and it was all in parts -
hundreds of little parts. So, we contacted our production-engineering group and
determined that they had some people that could probably assemble the engine in
a day or two. It took them about
three weeks. Many of the necessary
parts were missing and manufacturing had to fabricate some replacements.
This gave our
engineering staff time to evaluate what we needed in order to conduct the test.
We had been orally told that the new engine was designed to work with a
specific type of carburetor. But
how do you mount it, how do you control it, and many other “how to”
questions had been raised. It was
easy for us to fabricate some engine mounts and adapters through which we could
control and apply a load to the engine, but almost everything else required a
lot of special work. To make a longer
story short, it took us four weeks in the test lab before we finally got the
engine to run, but it would immediately stall when you just started to apply the
smallest load. Even without any
load, the engine consumed gasoline like crazy, and the rotor compression was
very low and erratic. By that time,
we had overrun the corporate budget by about 500%, so when the rotor compression
problem reoccurred for the tenth time, we called it quits and politely made a
recommendation to send the engine back for a lot more design work.
After we had
gotten a lot of smarts under our belts, the marketing department of our Northrop
division decided to bid on a major future Army contract which called for the
development of a rugged computer-controlled engine analyzer. We actually had
done a lot of homework in the right areas, including some work on the specific
engines involved. We had built a
prototype of an engine analyzer for the 4-cylinder Jeep engine and had the test
data from two-dozen so-called “operational” jeeps located at the El Toro
Marine base. These were Jeeps that
were supposedly ready to use. In
our opinion, almost half of those Jeeps had been misadjusted or had actual
failures that could easily lead to on-the-road full engine failures. If the vehicle is
supposed to be ready to use and then it fails, there were a lot of concerns
about the cost of being operationally ready.
Even when it has been reported to be defective, it was quite clear that
without some help, the young, (even well trained mechanics), were making a lot
of erroneous decisions about what needed to be replaced in order to return that
vehicle into the status of being in good operating order.
The need was fiscally and operationally there, but what was the fiscally
and practical answer. Regular U.S.
Marine maintenance personnel, using our breadboard engine tester, had done most
of the testing on the jeeps at El Toro. They
then did the repairs and retested the vehicles. Everyone was impressed with the results.
The officers involved were extremely pleased and they provided us, in
writing, with support, but, of course, these are not the people that make
procurement decisions back in Detroit and Washington. The low bidder for
the engine analyzer Request for Proposal won the contract to build 6 prototype
testers. They had bid about 2.5
million, and our bid was 5.0 million. We
had felt that our bid was extremely low. Our parts list for the hardware alone would have cost us
almost 2 million. So we did not get
the contract, but soon it was clear that the Army Tank Automotive Command (TACOM)
was planning to cover their bets. We
were requested to submit a couple of proposals for less than $100,000 each, to
build a jeep engine analyzer, and a jeep vehicle vibration analyzer.
In about six
months we had that jeep engine analyzer up and running very well. So off to TACOM, north of Detroit, we head out for a
demonstration of our demo unit. We
did have our share of problems with this adventure.
First, we had decided to check the package containing the engine analyzer
as excess baggage. We had packed it
real well and added a number of labels on the outside to make sure it could not
get lost. But when we arrived in
Detroit, the box containing the engine analyzer did not appear at the United
Airlines baggage area. I am sure
you can picture the scene. We were
running around trying to find someone who was in charge or could start a search
for the missing analyzer. We soon
found someone that gave it a lot of attention but the answer came back, “we
can’t find it.” “We have
searched LA, we have thoroughly searched here, and have not been able to find
it.” We were assured
that they had contacted all possible designations for flights to other cities in
case the box was put on another airplane, but thus far they had not received any
reports back. So we decided that we
couldn’t do anything at the airport and went to the hotel to call and alert
the people at TACOM and back at the plant.
About 2 o’clock in the morning, we got a rap at our hotel room and
there was a United Airlines guy with our box.
They had figured out that TACOM often came in and picked up mail packages
from the planes and they might have seen the package with all these TACOM labels
on it and loaded it on their truck as well.
So we spent the rest of the night checking out the hardware. The next morning
we proceeded up to Troy, Michigan where TACOM is located.
The jeep TACOM had agreed to furnish was there and we installed our
simulated fault that had been selected to result in a clear indication of a
spark plug failure. We walked
through our portion of the presentation at least five times and everything
worked great. Two hours later,
the program review team arrives and got seated in the bleachers to watch the big
show. Now we will fast forward to
our part of the session. At the
appropriate time we were on. First,
we planned to drive the jeep with the simulated fault into the area in front of
the bleachers. But the driver could
not get the jeep started. I took
center stage and “fast talked” to the audience about what great things they
were about to see. Meanwhile, a
couple of Army technician’s pushed the jeep out onto the stage area. They still had not gotten the engine to start. As I continued to
prepare the audience for the demo which might now not come about, someone came
running up with a battery charger and they got the jeep engine running and then
shut it down. So now I started
through a step-by-step process of connecting the engine analyzer onto the
engine. I actually made a point of
highlighting that the existing vehicles that the army currently had in their
inventory did not have good access to make these sensor and control connections.
It came time, and
I pushed the START button on the analyzer and stepped back. From there on the analyzer would tell the jeep
operator/technician what to do. “Start
Engine.” “Idle at 600 RPM.”
The instructions sequenced through nicely and I would explain what the
analyzer was doing during each step. “Increase
Speed to 1200 RPM.” Everything
seems to be going well and at the end of the 3-minute test the results were
displayed. The lights came on. “Valve
Number 3 Defective.” Oops!
It should have said “Replace Spark Plug Number 3.” I was told later
that I handled the problem quite well, by reminding everyone about the
difficulty we had obtaining electrical synchronizations of the mechanical parts
of the engine. I looked at the TOP
DEAD CENTER sensor and sure enough it was located on the wrong side of the white
ink mark which was to tell the analyzer when the engine number cylinder was at
top dead center of its mechanical rotation.
I quickly relocated the sensor to the other side of the ink mark and
requested the operator to rerun the test. Of
course, it worked as designed the next time, and the next time, and the next
time. But I had missed my day of
fame - again. Now that we are
talking about Detroit, there was another “exciting” adventure that occurred
in that city that I should tell you about.
The city of Detroit had quite a large Chinatown section and they actually
had a reputation for cooking up some very good chop suey. At least my cohort Chuck Blaney told me that this was the
case. During one of our
trips to Detroit, Blaney decided to buy some Detroit chop suey and take it home
with him. No problem, so on the way
back to the airport we stopped off at a chop suey shop. Blaney went in and bought a dozen cartons of this local
delicacy. These containers were
still warm to the touch, and had been placed in two paper shopping bags. On the way to the
airport, I was already having second thoughts about the wisdom of doing this.
We turned in our rental car and headed for the United Airlines ticket
counter. I was heading for Los
Angeles, and Chuck was to take a different flight to Dallas, where he would make
a business call on a potential customer. As
we entered the airport lobby, I was carrying our two suitcases, Blaney’s and
mine. He was toting the two
shopping bags that held the cartons containing the chop suey.
We had walked quite a ways when someone stopped Blaney and told him that
something was leaking from one of his packages.
We looked back and there was a liquid trail of chop suey juice all the
way to the building entrance - probably all the way back to the trunk of the
rental car. So we moved off to
the side of the room and Blaney ran off to locate something to put the leaky
package into. I was left there with
the goods and charged with keeping people from walking through the slimy fluid
that trailed down the corridor. It seemed like an
hour had passed before Blaney finally returned, but it was more likely only 5
minutes or so. By that time, a
janitor had arrived and was beginning the process of mopping up the slimy mess.
Chuck and I turned our attention to repackaging the contents of the two
paper bags into some plastic garbage bags that he had located.
We learned that two of the cartons on the bottom of each bag had
collapsed and was leaking their fluid. We
threw those four crushed cartons into a trashcan and repackaged the rest of the
containers into the black plastic bags. I was quite
relieved when this was completed and I grabbed the two suitcases in order to
quickly fade into the hordes of surrounding passengers.
But as I started out, I looked back and Blaney had disappeared.
The two black bags were still there.
Evidently guilt had gotten to him and he was heading down the hall
searching for the janitor in order to give him a gratuity for cleaning up the
mess - and it was a real mess by then - everyone was walking right through it. We eventually
checked in for our respective flights and I went with Blaney to his assigned
gate carrying one of the chop suey bags. I
could feel the warmth coming from the cartons inside.
As we walked I was imagining that each of the cartons was ready to split
open and would soon disgorge all of the remaining fluids onto me.
But we made it to his gate without any further incident.
But that is not the last of the story, but the rest is hearsay. About a half hour
later, Blaney’s flight loaded and he carried the two bags onto the plane and
placed them under the seat. By then
even he could smell the chop suey he was carrying.
After takeoff, a stewardess came up to him and made a polite inquiry
about what he had in the bags. Actually she
already knew what was there and offered to store his chop suey in the aircrafts
refrigerator that was on the lower deck. That
solved the odor problem for the rest of that flight.
Of course, when Blaney arrived in Texas, it was again his problem.
I will not tell you about his attempts to contain the problem, but I will
tell you about his flight home. On his way back to
Los Angeles, he is not flying in a big well-equipped 747 aircraft (partially
Northrop built - the main fuselage). So
even though he had repackaged the chop suey into more secure containers, there
was clearly a major problem for the other passengers. At the end of this
escapade, Blaney was able to deliver 3 containers of chop suey to his spouse.
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